In 1976 the Federal EPA published a report that attempted for the
first time to assess the damage to the environment nationwide, due
to the use of salt (sodium chloride) deicer (1). The increasing use
of salt since the 1940s was shown to have a serious negative impact
upon roads and highways, bridges, motor vehicles, groundwaters,
vegetation and soils. Although the study did not pretend to be a
highly detailed cost / benefit analysis, enough quantitative
information was generated to call for research and development into
novel, nonpolluting deicers to replace salt.
Accordingly, the Federal Highway Administration (FHWA) undertook the
challenge by contracting to Bjorksten Research Laboratories, a
research institute located in Madison, Wisconsin. The culmination of
that work appeared as an FHWA report in 1980 (2). After having
explored the entire chemical periodic table of the elements, and
based upon both technical and economic guidelines, Bjorksten emerged
with a chemical known as calcium magnesium acetate, or CMA.
Preliminary laboratory and field data were developed to show that
CMA was relatively non- corrosive, and an effective deicer.
The choice of CMA out of the several candidates examined was based
partly upon the assumption that the acetic acid raw material to be
used in its manufacture would be economically derived from wood and
paper components of solid waste. This is the so-called biomass or
bacteriological route.
The FHWA proceeded to examine the biomass approach by contracting to
Stamford Research International (SRI). SRI examined the capital and
operating costs of a selected bacterial route, based upon certain
assumptions concerning the operability of a particular bacterial
system (3). The projected operating costs at that time were only
slightly lower than those associated with the subject of the present
paper. However, the capital costs were at least an order of
magnitude greater than those which will be discussed in connection
with the present address. Currently, as a result of inflationary
pressures, even operating costs of the bacterial route offer no
incentives over the scheme to be presented herein.
It is our opinion that the bacterial approach, although conceptually
attractive, falls down on two accounts:
1.
The process itself is complex, requiring many steps and extensive
process control; and
2. A relatively dilute solution of CMA is the final product of the
scheme, and this must be converted to solid CMA through a costly
evaporation step.
Although researchers continue to explore bacterial approaches to
acetic acid, to date a technically successful and economically
attractive route to CMA does not exist.
THE SOLUTION ROUTE TO CMA
With the recognition that the bacterial route to CMA, even if it
were successful, would take large amounts of capital and a long
period for development, the FHWA sponsored the production of CMA
from merchant acetic acid and dolomitic lime (4). The purpose of
this program was to produce 200 tons of material to be used by
selected state highway departments for expanded wintertime field
testing. In this approach, a concentrated liquor was produced
through batchwise reaction of dolomitic lime and acetic acid. The
system was settled with the aid of surfactants, and then filtered.
The solution was then superfiltered so as not to clog the spray
nozzles used in the subsequent fluidized bed drying operation.
Production of the 200 tons was successful. However, product
characteristics were unsuitable for effective deicer end use. In the
course of the higher temperature evaporation process, substantial
hydrolysis occurred:CMA
+ water ---> Basic Acetates + (volatile) Acetic Acid.
The consequences of hydrolysis were two:
1. CMA product pH was around 10 instead of the desired range of
7-9. This was due to volatilization of costly acetic acid in the
process.
2. Product insolubles were undesirably high at approximately 5%,
due to precipitation of basic acetates (or other basic products)
formed during hydrolysis.
Additionally, CMA product was too fine and dusty.
It was also undesirably friable. However, even if undesirable
physical attributes were correctable, the consequences of hydrolysis
would remain.
It is even conceptually possible to inhibit the hydrolysis
phenomenon but not without costly acid losses. But one of the major
drawbacks to the 200-ton CMA production program was the fact that it
was a five-step process. Process complexity was reflected in the
capital and operating costs. For example, the cost of a 1000-TPD
plant was $74 million, with operating costs at 32¢/lb for CMA
in 1984 dollars. By contrast, rock salt sells for about 1¢/lb.
The largest cost factor is raw material acetic acid, which accounts
for 16-20¢/lb of CMA product. This factor is conceivably
reduced through large-volume discounts, and/or use of lower grade,
lower cost acid. In processing, however, the largest single cost is
that associated with evaporation of water in converting CMA solution
to solid product; this amounts to about 5¢/lb of CMA.
It was at once evident that a new process was required which:
1. was simple in conception so as to reduce capital costs
significantly below any conceived heretofore, and
2. required little or no water evaporation.
THE PATENTED GANCY CHEMICAL ROUTE TO CMA
A novel route to CMA was conceived that involved reacting dolomitic
lime directly with acetic acid solution containing a minimum amount
of water. The function of the water was to aid in reaction heat
dissipation, and to distribute the acid. Using this approach meant
that the CMA would contain all of the insoluble impurities present
in the lime. The impurity dilution factor, on an anhydrous basis,
would be 0.32 due to the large difference in molecular weight
between raw material and product.
Thus a lime containing 1% insolubles would result in a CMA product
containing 0.32% insolubles. This was considered an acceptable
compromise for a product which, after all, required no high degree
of purity both for functional and even environmental reasons.
The first attempt to reduce this approach to practice in the
laboratory resulted in disappointment. It was a batch process in
which acetic acid solution was slowly fed to a stirred batch of
dolomitic lime. The calcium oxide component of the lime reacted
preferentially to the magnesium oxide component, with the evolution
of considerable heat.
During the early stage of the reaction, the batch was free flowing.
However, as more of the MgO began to be converted to the acetate
during the latter stage of reaction, the batch became sticky, and
the stirrer would tend to seize up. This reflects the well-known
highly viscous nature of concentrated (aqueous) magnesium acetate
solutions. The sticking problem was not solved by varying the level
of water input.
It was evident that a scheme was required which reacted each
dolomite component completely with acetic acid during the entire
course of the process. A laboratory scheme was therefore developed
in which stoichiometric equivalents of lime and acid were
simultaneously introduced to the reactor, in a semibatch mode.
Initial streams were directed into a small stirred heel of product
deriving from previous unsatisfactory attempts.
The continuous approach was successful. Water input was adjusted
such that there was no stickiness throughout the course of the
process. At the same time, sufficient water was used to:
1. minimize encapsulation of lime by product CMA;
2.
minimize heat buildup, which would tend to volatilize unreacted
acetic acid; and
3. eliminate dustiness.
The product emerged as pea-size imperfect pellets, or chunks.
Raw material and product were carefully weighed to determine water
lost through evaporation. Product was then optionally equilibrated
with air at room temperature to determine the degree of hydration of
product.
The successful reaction formula was found to be CaO.MgO + (4HAc
+3H2O) ---- >Product. In other words, an 81.6% acetic acid
solution was reacted with dry dolomite. Incidentally, this approach
allowed one to use unslaked dolomite, a minor cost saving over all
previous approaches to the problem.
A 5% stoichiometric excess of acid was generally used in order to
counteract any hydrolysis, and to ensure as complete a utilization
of lime as possible, considering the potentials of acetic acid
volatilization. Using this approach, the product CMA always had an
odor of acetic acid. This odor was easily removed by oven-drying
product CMA to constant weight at 100°C. The resulting product
empirical formula was:
Ca(Ac)2·1.05
Mg (Ac) 2·0.4H2O
The water content was determined by carbon-hydrogen analysis. The
residual water level was independently confirmed as the stubborn
affinity of magnesium acetate for water. In fact, without excess
acid present, damp magnesium acetate was shown to hydrolyze
significantly during drying.
Yet CMA appeared to be not a simple mixture of the known compounds
calcium acetate and magnesium acetate (tetrahydrate). In fact,
careful laboratory scale experiments were performed in which
sufficient input water was introduced to allow the tetrahydrate to
form. When such preparations were air-dried to constant weight, the
resultant empirical formula was:
Ca(Ac) 2·Mg(Ac)2·2H2O, and not:
Ca(Ac)
2·Mg(Ac)2·4H2O
as may have been expected. Without x-ray diffraction or other
analytical data as evidence, this leads to the tentative conclusion
that the product formed through lime-acid neutralization is a
chemical compounding of calcium and magnesium acetates. This was to
prove important in subsequent programs in which the mol ratio of
magnesium to calcium in the products was deliberately varied over
the whole range possible.
It was evident that a low-cost process had now been developed in
the laboratory that had potential for success using commercially
available industrial-scale pelletizing hardware.
REACTION MECHANISM
It is worthwhile commenting on some of the subtleties of the
complex series of reactions thath make the entire process possible.
It was mentioned earlier that lime encapsulation can be a serious
problem. This was found to be true whether or not the lime was
slaked prior to reaction. Incidentally, without resort to a
pressure process, it is only the CaO component of dolomite that is
slaked:
CaO·MgO + 2H2O ---- >Ca(OH) 2·MgO + H2O
Independent studies showed that the water input level was critical
to avoid such encapsulation and consequent incomplete reaction of
the lime. Even use of a stoichiometric excess of acid would not
ensure complete lime utilization, if the water input level did not
exceed a certain critical minimum.
On the other hand, too large an input level of water would
obviously create a "wet" batch. This has undesirable
consequences for pelletizing. But it also means a potential CMA
product drying step which is to be avoided, if possible.
For the solution processes discussed earlier, about 50 mols of
water must be evaporated for each mol of (anhydrous) CMA produced.
In the present scheme, no more than 5 mols of water are associated
with CMA. Of these, approximately two are volatized during the
course of the exothermic reaction, leaving about 2-3 mols
associated with the product.
These 2-3 mols of water can be largely eliminated by drying; this
contrasts importantly with the 50 mols which must be removed in all
solution processes.
It is extremely important to note that the product intermediate
containing 2-3 mols of water is plastic at the temperature of a
typical reaction batch. This indeed is what makes the pelletizing
process possible at all. But when the product is cooled and allowed
to stand, it becomes rock hard. Experiments in which product was
stored in tightly sealed containers demonstrate that hardening is
not due to a partial air drying. Pellets become rock hard even when
forced to retain the 2-3 mols of water per mol of CMA. This, then,
is a clear demonstration of a slow crystallization process, and is
reminiscent of the behavior of magnesium acetate tetrahydrate.
The pure tetrahydrate melts at around 70°C; when it is cooled,
a glassy state is formed that is slow to recrystallize.
Thus CMA can be "cured" without a drying step after it
emerges from the pelletizer. Curing to a rock-hard product requires
one to two days. However, a separate curing operation is not
necessary; product can go straight to the stockpile, or to a bagging
operation where curing ultimately occurs automatically.
An oven-dried version of the new CMA product was found to be a
superior deicer in tests conducted at the FHWA laboratories in
Washington, D.C.
THE COMMERCIAL PELLETIZING OPERATION
Based upon the successful laboratory experience in producing and
pelletizing CMA in a single-unit operation, a proposal for proving
the concept on a pilot scale was made to the FHWA. A contract was
awarded, and the following describes the successful piloting of CMA
manufacture (5).
The process was not a straightforward pelletizing application, in
that the pelletizer had to provide thorough mixing of the dolomitic
lime and acetic acid to completely react and also to form
irregular-shaped pellets. The pelletizer had to:
· thoroughly mix the ingredients to assure complete reaction;
·
form shaped pellets with a similar size distribution as rock salt;
·
be unaffected by the high heat of reaction during the mix/reaction
stage;
·
be able to perform during the "molten" stage of reaction
to produce individual pellets instead of one large "pellet";
and
·
provide cooling and shaping time.
With these parameters in mind, we set out to determine if
agitation-type pelletizers
could be utilized.
Four types of agitation-type pelletizers were considered; Deep
Drum, Disc, Ampel Horizontal Pelletizer/Conditioner and Pin Mixer.
The Pin Mixer was not chosen for testing due to its short retention
time and inability to produce a larger particle size product of 5
mesh, to conform to rock salt sizing. The Pin Mixer would provide
excellent mixing but the energy requirement and wear considerations
made it the least preferred method of agglomeration.
The Disc Pelletizer was tested, and also proved to be inadequate
for the reaction and formation of CMA pellets. The low retention
time and the inability to establish normal growth patterns on the
Disc led to control problems that could not be stabilized. The
pellets produced were too small to be comparable to rock salt. The
resulting -10 +16 mesh pellets could not be easily increased in
size.
The Ampel Horizontal Pelletizer/Conditioner was also tested. The
Ampel could be controlled, and definite zones were established
within the unit; ie, mixing/reaction zone, pellet-formation zone and
cooling/ finishing zone. Pellet size, however, was difficult to
control. Large pellets were formed, up to 1" diameter, that
would require size reduction to meet product specifications.
Continued operation of the Ampel resulted in excessive build-up of
materials inside the unit, rendering the mixing paddles useless.
The Deep Drum Pelletizer was also tested and proved to be the
preferred device for the agglomeration of CMA. Initial testing was
performed on a laboratory-size Deep Drum Pelletizer with drum
dimensions of 14" diameter by 9" deep.
As with all of the test work, the dolomitic lime was added
continuously to the pelletizer while a spray of acetic acid solution
was being applied. The Deep Drum Pelletizer allowed the materials to
be mixed, provided a reaction zone and a pellet formation/cooling
zone. The advantage of the Deep Drum Pelletizer over the other
pelletizing devices tested was that pellets could be continually
produced within the desired particle size range.
As a comparison of particle sizing of rock salt and pelletized CMA,
a sizing test was performed on a Forney sieve shaker on commercially
available rock salt and pelletized CMA from a Deep Drum Pelletizer.
The analysis was as follows:
Rock
Salt Pelletized CMA
(% Retained) (% Retained)
+ 5 mesh 12.3 46.1
+ 7 mesh 22.5 43.9
+ 10 mesh 18.3 8.9
+ 20 mesh 29.9 1.0
+ 45 mesh 11.6 .1
+ 60 mesh 1.3 0
- 60 mesh 4.1 0
The
pelletized product had a tighter range of particle sizing than rock
salt and virtually eliminated the minus 45 mesh fraction. The CMA
centers on the largest of the rock salt particles in the sample and
this was judged to be a satisfactory result. It is possible to
regulate pellet size produced in the Drum Pelletizer by adjusting
the operating angle of the drum and/or by increasing feed rates. The
increase or decrease of retention time will affect agglomerate size.
The next step in the evaluation of the Deep Drum Pelletizer was to
upgrade the test work to a production-size unit. The Model D-20 unit
was chosen, which has a drum dimension of 2'-0 diameter by 1'-4"
deep or a depth-to-diameter ratio of 0.66.
The pelletizer is equipped with an integral feeder that introduces
the feed material at the rear center of the drum, where the initial
mixing/reaction with the acetic acid occurs. The rotating drum
continually agitates the feed material for even acid distribution
and to promote pellet formation and growth.
The critical concern at initial pellet formation stages is to avoid
the encapsulation of unreacted dolomitic lime. This was controlled
by varying the dilution ratio of the acetic acid within narrow
limits to increase or decrease the reactivity with the dolomitic
lime. Higher dilution rates slowed the reaction, allowing the
dolomitic lime to be reacted before encapsulation occurred.
The acetic acid was introduced to the pelletizer through a spray
system with three fan-type spraying nozzles. The location of the
spray points inside the drum pelletizer was variable. One spray was
directed to the rear of the pelletizing drum where the feed enters
to initially react with the lime and to form seed pellets. The
second two were positioned to further coat the seed pellets to
promote pellet growth. The formed pellets were then rolled in the
outer portions of the Deep Drum where they cooled and were
continually discharged.
The operation of the Deep Drum Pelletizer resembled usual
applications. The major difference was the violent reaction of the
acid and lime, which caused heat and vapor, that at times made it
nearly impossible to visually observe what was taking place inside
the drum. Seed pellet formation and progressive growth were normal
as long as the proper ratio of acid to lime was maintained. An
inadvertent excess acid addition made the pellet bed inside the drum
too molten and large agglomerates were formed. Maintaining of the
proper stoichiometric ratios, however, eliminated this problem.
A pilot plant was constructed at the Mars Mineral (MMC) laboratory
to demonstrate the capabilities of the Deep Drum Pelletizer during
sustained production runs. The plant consisted of a small storage
bin for the dolomitic lime that fed into the pelletizer feeder
inlet, D-20 Deep Drum Pelletizer, discharge product cooling belt
conveyor, rotary dryer, vibrating screen and bagging station. The
acetic acid was pumped from containers through a diaphragm pump into
the pelletizer spray system. In order to better maintain the ratio
of acid to dolomitic lime, a volumetric screw feeder was later
inserted between the lime storage and the pelletizer inlet to
provide a more accurate feed flow.
The rotary dryer was placed into the system to dissipate the excess
acid from the pellets. The dryer was a smooth-bore rotary type, 22"
diameter by 22'-0 long, gas-fired with counter current flow. The
exiting pellet temperature was approximately 70°C.
The pelletized CMA was discharged from the dryer to a vibrating
screen that removed oversize and undersize pellets. The undersize
was the product of attrition through the dryer and screen. A test
was performed to determine the attrition losses of on-size product.
ASTM D4058-81 was used to measure the attrition properties of dried
CMA product and of dried rock salt. In this test, the dried material
is gently sieved on a No. 20 mesh sieve to remove fines, then fed to
a closed cylindrical vessel containing a single radial baffle
extending the full length of the cylinder. After 30 minutes at 60
rpm rotation, the sample is removed and sieved again. The difference
between the before and after weights is a measure of the attrition
rate.
ATTRITION
TEST
ASTM D4058-81
Sample Sub-Sample Attrition, % Average, % Rock
Salt 1 5.6 2 6.5 6.0
CMA 1 5.3 2 3.5 4.7 3 5.3
The
attrition rate for pilot plant CMA is seen to be comparable to rock
salt, if not better.
The screened product was then fed to a bin over a valve-type bagger
and packaged in 25-pound poly bags for shipment. The product handled
well through the bagger with little or no additional attrition
losses.
The pilot plant was operated to produce approximately 3000 pounds
of CMA that was sent to various locations for product evaluation.
The results of the field test work have not been completely
evaluated at the time of this presentation. Preliminary data
indicate mixed reactions from the end users. The comments received
ranged from product sizing to ice-melting capabilities at lower
temperatures. These are both areas in which adjustments can be made
to the process to make a product to meet individual customer
specifications.
In conclusion, the above-described work has shown that the
production of CMA pellets can be achieved on an agitation-type
pelletizer:
· Four industrial pelletizers were evaluated, which led to
the selection of the Deep Drum Pelletizer as suitable for carrying
out the synthesis and agglomeration of calcium magnesium acetate in
one step.
· Reaction chemistry, as performed in the laboratory, was
found to be directly translatable to pilot operations.
· The CMA product produced in the pilot plant was comparable
to the laboratory-produced material in most aspects, excepting that
it was less dusty and less friable. This may be due to a
case-hardening phenomenon resulting from the tumbling of CMA
agglomerates in the pelletizer.
· Particle size distribution of CMA product was very narrow
and centered on the largest of the particles in a commercial rock
salt. Attrition resistance of this material is comparable to, or
even better than, rock salt.
The agglomerates produced were irregular in shape, which is an
advantage when applied to hard surfaces from moving vehicles, or to
surfaces for pedestrian traffic. The irregular shape reduces the
ability of the agglomerate to roll off the surface, and provides
stable footing.
Solution tests on CMA product reflect a high degree of reaction
completion, with a minimum of insolubles, and a desirable pH of 7.4.
Chemical analysis of dried CMA product indicates that at least 0.2
mol of hydration water per mol of contained calcium acetate is
retained.
Capital cost for an 80,000-tpy plant is estimated to be $3 million.
Fixed and variable operating costs are approximately 5.5¢/lb
over and above the cost of the acetic acid input. As in all
processes employing merchant acetic acid, the acid input cost is the
dominant operating factor. A significant feature in the pelletizing
process is the fuel requirement of about 0.6¢/lb CMA. This is
to be contrasted to the cost of evaporating a CMA solution to
dryness, a figure approaching 5¢/lb CMA.
This paper has presented a pelletizing application that, in our
estimation, was unique and not typical of mainstream agitation
pelletizing. The results are from the evaluation of only four of the
available agitation-type pelletizers and is not to say that other
types or processes would not produce an acceptable product.
The goal of selecting a pelletizing device to produce CMA was
indeed reached by using an "off-the-shelf" pelletizer,
with little or no modifications required.
REFERENCES
1.
Murray, D. M., Ernst, V. F. W., "An Economic Analysis of the
Environmental Impact of Highway Deicing." EPA 600/2-76-105
2. "Alternate Highway Deicing Chemicals." FHWA-RD-79-108
3. "Process Development for Production of Calcium Magnesium
Acetate (CMA),"
FHWA-RD-82/145
4. "Production of Calcium Magnesium Acetate (CMA) for Field
Trials."
FHWA-RD-83/062
5. "Preparation of High-Quality Calcium Magnesium Acetate
Using a Pilot Plant Process." FHWA Contract No.
DTFH61-84-P-10011